Thermostat housing leak after replacement
Well we finally caught a break on weather today so after I got home from work I started working on the truck. The sealer had about 3 full days to cure so I expected it to be nice and water tight. I hooked everything back up, fired up the truck, and it still leaked. I couldn't believe it! Shortly after trying to find how it could possibly be leaking, I discovered a loose hose clamp on the heater hose directly to the left of the thermostat... I'm a moron. I don't remember loosening it while pulling the thermostat the first time, but I must have. After tightening that back up and putting everything back together, I started the truck up and the leak was gone. I ran the truck for a bit and while the heat is definitely much improved, it still seems a tad low. I'm going to flush, fill, and do a proper burp on the system this weekend as I'm sure I let a ton of air in throughout the process. If that doesn't bring the heat up more I'll probably flush the core, and hopefully call it a day!
Glad to report my heat is now fixed and blowing hot! Earlier today I got around to flushing the heater core. One of the hoses was brittle and split when pulling it off, so I got some new hose at the parts store and replaced it. I flushed the heater core thoroughly both ways and multiple times. I caught all the gunk that came out with a water jug and it was filthy and very dark gray in color. After that, I also found the cause of my temp gauge showing low. While removing one of the heater hoses to the left of the thermostat I went to unplug an electrical sensor for more room. I then discovered the plastic top of the sensor popped right off and was broken. After checking the service manual I found it was the Coolant temperature switch/sender. I ran to Autozone first and bought one, but after comparing with the original the threading and length, found it was too long. FYI The part from Autozone was a Duralast TU165. I then headed over to Advance Auto parts and got a correct replacement which was a BWD WT427, and it fit perfect. After putting everything back together and tightening it all down, I flushed the whole system 3 times with water, which removed even more gunk. I filled it back up with coolant and all is well. Thanks to all for the advice and help! This board has been an invaluable for all my repairs so far.


