2nd Gen Dakota Tech 1997 - 2004 Dodge Dakota Tech - The ultimate forum for technical help on the 2nd Gen Dakota.

My First Engine Swap

Thread Tools
 
Search this Thread
 
Old Oct 7, 2013 | 07:48 AM
  #101  
sxrsil3nt's Avatar
sxrsil3nt
Thread Starter
|
Record Breaker
Joined: Dec 2010
Posts: 1,075
Likes: 3
From: Ontario, Canada
Default

Originally Posted by Brian in Tucson
The trannie will either survive or it won't. In which case you'll have to head back to the wrecking yard for a replacement one. Water in an auto transmission is not a good thing.

Don't tell me that Brian.

We're hoping for the best here!
 
Reply
Old Oct 21, 2013 | 01:31 PM
  #102  
sxrsil3nt's Avatar
sxrsil3nt
Thread Starter
|
Record Breaker
Joined: Dec 2010
Posts: 1,075
Likes: 3
From: Ontario, Canada
Default

Well after a few weeks of driving it the tranny is starting to slip in second... doesn't always downshift to first... and clunks hard into 4th.

I think she's just about toast boys.
 
Reply
Old Oct 21, 2013 | 01:36 PM
  #103  
magnethead's Avatar
magnethead
Legend
20 Year Member
Photogenic
Liked
Loved
Joined: Feb 2005
Posts: 8,058
Likes: 183
From: Fort Worth, TX
Default

4th is an auxbox, if it's going in hard then the convertor isn't unlocking between gears.

If you're brave, I would say drop the trans pan and open the valve body, and check all the checkballs and springs. Maybe some mud and sludge got in there and is making stuff stick.
 
Reply
Old Oct 21, 2013 | 01:51 PM
  #104  
sxrsil3nt's Avatar
sxrsil3nt
Thread Starter
|
Record Breaker
Joined: Dec 2010
Posts: 1,075
Likes: 3
From: Ontario, Canada
Default

Just about everyone I've talked to said its toast since I got water in the tranny.

It was only a matter of time but I was hoping for more than 3 weeks that's for sure.
 
Reply
Old Nov 6, 2013 | 01:07 PM
  #105  
sxrsil3nt's Avatar
sxrsil3nt
Thread Starter
|
Record Breaker
Joined: Dec 2010
Posts: 1,075
Likes: 3
From: Ontario, Canada
Default

November 6th, 2013 Update

I've been driving the truck for about a month now and everything has been good except for a small hickup with the torque converter bolts. I didnt apply locktite when I am tightened them and as a result they ended up vibrating loose and making a rattling noise. Kids, use your locktite.

The transmission has also greatly improved with a good drive cycle. It will still sometimes not downshift to first, or sometimes you'll come to a complete stop and about 3 seconds later it would downshift and sort of jerk the truck forward.

I'm now beginning to think I have an issue in my valve body, possibly the Throttle valve. I have a stiff gas pedal with the TV cable connected, but I've ruled out a problem with the actual cable itself. I'm pretty sure something is sticking or binding internally in the transmission.

Haven't noticed anymore slipping between gears, 1-2 was most noticable but it appears to have settled down.
 

Last edited by sxrsil3nt; Nov 6, 2013 at 07:42 PM.
Reply
Old Nov 6, 2013 | 05:09 PM
  #106  
Brian in Tucson's Avatar
Brian in Tucson
All Star
Joined: Mar 2013
Posts: 783
Likes: 0
From: Eastside Tucson AZ
Default

Originally Posted by sxrsil3nt
November 11th, 2013 Update

Gosh, you Canadian take going off Daylight Savings time very seriously.
 
Reply
Old Nov 6, 2013 | 07:48 PM
  #107  
sxrsil3nt's Avatar
sxrsil3nt
Thread Starter
|
Record Breaker
Joined: Dec 2010
Posts: 1,075
Likes: 3
From: Ontario, Canada
Default

Originally Posted by Brian in Tucson
Gosh, you Canadian take going off Daylight Savings time very seriously.

LOL

Oh man I had the date right infront of me and I still screwed it up.

I've edited it now... THanks Brian lol
 
Reply
Old Jan 12, 2014 | 10:08 PM
  #108  
sxrsil3nt's Avatar
sxrsil3nt
Thread Starter
|
Record Breaker
Joined: Dec 2010
Posts: 1,075
Likes: 3
From: Ontario, Canada
Default

January 12th, 2014 Update (Brian, did I get the date right?? Hahaha)

Well she's made it into the new year boys!

Since my last post I had dropped the tranny pan for a second time and replaced the fluid. Truck has been giving me no powertrain problems - ran into a slight coolant leak but that was my fault not securing the lower rad hose properly.

A few issues with my powersteering pump and a clunk that I can't find but it runs and shifts smooth. I've got a bearing (likely the alternator) that's very noisy but the truck runs fine otherwise.

Thanks again for checking in!
 
Reply




All times are GMT -4. The time now is 01:13 AM.