Neon SRT-4 Dodge Neon SRT-4 is the pocket rocket that took the import scene and turned it upside down.

anyone else experience this??

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  #11  
Old 12-16-2006 | 07:09 PM
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ORIGINAL: PSI Chick

lol no he probably had no idea why it was freaking out and made something up so he didn't sound like an idiot
yeah, so now i sound like the dumbass. thanks there sevice manager[:'(]
 
  #12  
Old 12-17-2006 | 11:58 AM
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same thing happened to me, put on a boost contoller and was spiking too high so 3 hoses blew out(dumbass)....had to use the e-brake, eventually I putted clamps and Tie racks on all of them..haven't happened ever since
 
  #13  
Old 12-17-2006 | 07:36 PM
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why would you need to use your ebrake? when experiencing this problem the brakes worked fine, just throw the car in neutral and let it rev itself until its content.
 
  #14  
Old 12-18-2006 | 01:45 PM
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not really bro....remember 3 hoses blew out....one of them had to do with the brakes and i was going 40mph and a red light up ahead.when i parked the car kept reving for about 30 sec then i shut the car off and tied all 3 hoses back.
 
  #15  
Old 12-18-2006 | 04:18 PM
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you blew the brake booster line. that's unrelated to the tps issue.
 
  #16  
Old 12-18-2006 | 05:08 PM
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that's the cause to my car idling funny though i know 4 sure. could it possibly be the casue of loss of boost? i mean it is a vacuum hose??right?
 
  #17  
Old 12-18-2006 | 05:25 PM
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the tps sensor you mean? if it fell out of the hole, then sure. otherwise, no.
 
  #18  
Old 12-18-2006 | 07:40 PM
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it didnt fall...it broke. so i need to know if i have to replace the whole vacuum rail or what my options are...superglue didnt work very long
 
  #19  
Old 12-19-2006 | 02:54 AM
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the sensor itself broke???? how did that happen??? you have to replace the sensor then....
 
  #20  
Old 12-19-2006 | 01:59 PM
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its not the sensor. follow your # 3 sensor from the intake box down to the turbo. (its a blue hose). at the other end it connects to the vaccum port coming off the turbo right below the stock converter valve. i cant remember the correct terminology for it, but there is a plastic tit that the rubber nipple fits right over. that tit is what broke off inside the nipple..if anyone could give me that correct terminology so i could call the dealer and get a new one that would be great. if you have the mopar BOV conversion kit its the #6 part on the picture of the turbo on the backside of the installation instructions
 



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