Smoking, missing and ****ing firm...here we go
#21
Showing 15 ohms on inj 2...compared to inj 4 and they are consitant. I have #2 unhooked atm while the truck is running and it makes no difference in idle if I plug/unplug/plug back in. I'm gonna go see if I can get a fuel pressure tester at the Zone. I'm gonna leave it unplugged for now so Im not washing out the cyl...
Gonna p/u a tps also
Gonna p/u a tps also
#23
Tried to fix it and couldn't, was too late haha
Well I found a tester (loaner tool) and as nice as it was, it didn't have the adapter hose that I needed. I'm gonna go try another parts store. Had to run back home and get my wallet...whata day. Had today off for some recovery time from a monor surgery (major to us men) but it aint so bad. Just trying to get done what I can while I have this day. So please stay posted and thanks for all the help
Last edited by Dantra; 12-06-2010 at 03:36 PM.
#26
Got it...damn boogers.
O-rings, do they go on the inner groove or out on the nipple? They're getting left behind as they come out.
Im gonna swap 2 and 4
EDIT...before dropping back into the manifold I turn the key on, with nothing electrical plugged in. One injecter has a steady drip. Guess thats no good
O-rings, do they go on the inner groove or out on the nipple? They're getting left behind as they come out.
Im gonna swap 2 and 4
EDIT...before dropping back into the manifold I turn the key on, with nothing electrical plugged in. One injecter has a steady drip. Guess thats no good
Last edited by Dantra; 12-06-2010 at 04:42 PM.
#29
Dug through a pile of injectors and found a very close match ( I bought a new one as well...just in case)
Runs ALOT better. Still not 100% but is better by leaps and bounds. I believe if I found the TSB and maybe dig a little deeper into the #5 misfire that it'll be gooder than almost new. I'll clear the codes tomorrow and see what shows up. But for now it runs better, shifts better and only has a slight vibration in OD. I can deal with it till it warms up outta the single digits
Thanks for the help on this go 'round
Runs ALOT better. Still not 100% but is better by leaps and bounds. I believe if I found the TSB and maybe dig a little deeper into the #5 misfire that it'll be gooder than almost new. I'll clear the codes tomorrow and see what shows up. But for now it runs better, shifts better and only has a slight vibration in OD. I can deal with it till it warms up outta the single digits
Thanks for the help on this go 'round