The Official 2nd Gen RAM Forum OT thread
#7887
LOL. TFT Matrix is a special type of LCD screen. Much better contrast, sharper colors, and better 3D. IBM is the almost exclusive user of them.
There are three main types of spark plug wires: Street (Red), Strip (Yellow), and Racing (Blue). The color codes are from the brand I use (Belden, which is carried at most NAPA stores). They are all listed as 8MM wires, but there is a difference. Street uses a metallic conductor. I do not know what conductor strip uses, because I have never needed to use spark plug wires in a strip application. The Racing grade (Blue) is a 8MM non-metallic conductor, with extra shielding. It has a larger core than most standard wires, thus enabling it to transmit higher voltage. I chose this because it is a significant improvement over most street styles with the different core, better insulation, and higher capacity. Between the racing and premium street styles, I have noticed a big difference in spark strength. It's ideal for running a stronger coil too. Here's the set I got: http://www.napaonline.com/Catalog/Ca...614_0267518052
I did the kegger mod when I replaced the plenum plate and gasket. That was before the transmission went out.
I'm trying to find the picture LOL. I'm certain I posted a pic somewhere on DF, but can't seem to find it.
What difference did it make? For one it got my power band in a acceptible location (2500-3500RPM, instead of over 4000RPM). I also replaced my heads while I was at this, so the heads might have made a difference. And I also put on true dual exhaust. So how much effect the plenum mod exactly had, I don't know. It was enough reduction in restriction in the intake that it cause the MAP sensor vacuum reading to cause the computer to think it is under load (I verified this with a OTC tool). So be careful - you'll need a tune to compensate for this if it happens. This is why my truck is running rich too. All in all, I would do the plenum mod even if it didn't seem to make a difference. I am also running a 180* tstat without a tune and having no problems with it.
So bottom line here, whatever the combination of the above, it had a amazing effect on the performance. Before it was always slow to accelerate - after, it would put-you-back in the seat with ease. But that was probably why the transmission went out shortly thereafter.
Helpful explanation?
I did the kegger mod when I replaced the plenum plate and gasket. That was before the transmission went out.
I'm trying to find the picture LOL. I'm certain I posted a pic somewhere on DF, but can't seem to find it.
What difference did it make? For one it got my power band in a acceptible location (2500-3500RPM, instead of over 4000RPM). I also replaced my heads while I was at this, so the heads might have made a difference. And I also put on true dual exhaust. So how much effect the plenum mod exactly had, I don't know. It was enough reduction in restriction in the intake that it cause the MAP sensor vacuum reading to cause the computer to think it is under load (I verified this with a OTC tool). So be careful - you'll need a tune to compensate for this if it happens. This is why my truck is running rich too. All in all, I would do the plenum mod even if it didn't seem to make a difference. I am also running a 180* tstat without a tune and having no problems with it.
So bottom line here, whatever the combination of the above, it had a amazing effect on the performance. Before it was always slow to accelerate - after, it would put-you-back in the seat with ease. But that was probably why the transmission went out shortly thereafter.
Helpful explanation?
#7888
Join Date: Mar 2011
Location: Fredericksburg, Virginia
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@merc: What happened is I was in the kitchen running water and water pressure was terrible, almost none.
Went outside and heard water, there's a screw cape a little further up the piping that had either been blown out or came loose, and water was gushing out of it, so I screwed it back in, wasn't sure what had happened, so I turned the boiler on, it ran fine (and still does) and then I heard water again, and the case was cracked on the Circulator.
Went outside and heard water, there's a screw cape a little further up the piping that had either been blown out or came loose, and water was gushing out of it, so I screwed it back in, wasn't sure what had happened, so I turned the boiler on, it ran fine (and still does) and then I heard water again, and the case was cracked on the Circulator.